Video from Leota Michigan on our 400's 5-30-2020 Was A nice Afternoon.
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By Dumass
My name says it all. I have a '03 Honda Sporttrax 400EX with a new aftermarket carb on it that seems to be having issues. I can start it but it idles really rough and when I give it throttle it just kills the engine. I have tried adjusting the idle screw but to no avail. I am in the San Diego Ca area.
Any advice will be greatly appreciated. I would also like to get an owners manual for the thing too but can't seem to find a downloadable one.
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By Trent Finnessey
I’ve got a 2000 400ex with a dg slip on muffler, it came with he stock muffler on it but the previous owner had the dg in a box so I put it on. I’ve been riding it for the past month and a half and every time I let off it backfires, and the other day the backfires got way louder, 2x louder! I’m concerned that I may hurt my motor? Why does is backfire??? Thanks
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By Arizona
I recently bought a 87 TRX 250 not running of course, the owner had a brand new Key Switch on it.
I think it is the wrong one or wrong wire colors as the colors dont match up with wiring diagram i downloaded for it.
anyone have a pic of their ign switch wires where they connect with the wire colors for that model? I ended up leaving the black/w stripe and
green wire disconnected in order to hot wire it for other testing but would like to know as the colors dont match diagram.
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By Ejwill
Well while I was waiting for new parts for the choke, I decided to adjust the clutch. When I removed the lock nut, I found the guy I bought it from or someone else had stripped the threads on the adjustment rod. I couldn’t get the adjustment rod to turn without putting a pair of channel locks on the screw driver, this was telling me something was wrong. So now the rod pushes in and out and spins freely too freely. So guess I’ll have to take the clutch housing off to see what’s going on and replace the adjustment rod, it’s threads are beyond repair, and there is something going on with the adjustment rod. If there’s another way please let me know. The further I go the worse it gets. Thanks for any help.
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By Ejwill
I put a new carb on my trx500fe which I have done before on other models, but this foreman was a real pain, takes forever to get to the carb. Anyway I got the new one installed . I also changed the choke cable while I had it this far. When I turned the gas back gas started running into the air filter box. I did have trouble with the choke cable, it didn’t seem long enough to run where the old one did and the elbow that came with the new carb had more of a 90 on the angle. It didn’t feel like it was binding but I don’t know if the valve was seated on the valve seat. The choke pushed in smooth but who knows what happened in side the valve body. I don’t know if this could be the problem or not I hadn’t run the it just turned the gas back on. Appreciate any help, hint, hint Mech and GW or anybody else. Deer season is over in a little over a week. My power chair won’t make it down those muddy roads. Thanks again.
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